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rick t

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Posts posted by rick t

  1. With the RCBS bullet feeder you lose a die and I like to run powder check and taper crimp die. I did run some with the RCBS die and worked fine, no problem with the bullet when it indexes. The Lee holds the bullet up in the mouth of the die, then the case picks it up on the way to seat the bullet with no loss of a die. The collator won't work with cast bullets and makes a mess out of it!

  2. I have taught alot of people to reload in the last 30 years and I tell them "No question is a stupid one if you don't know the answer" on the other hand if it is the same one every time! Check the prices on the upgrade kits and do the math. I myself would wait and give yourself the best present of your life!!!!!!!!!!

  3. I had a extra hopper and just J-B Welded it on top of another one with the baffles in opposing directions. I was loading 300 win. mag. and got tired of filling it every 100 rds. I did that years ago and never had a problem with variation.

  4. I did all that with the plastic slip on things they work and work well. Then I broke down and got one of Lee Loves (Unique Tek) micrometer adjustments for my powder bar. I was sceptical whether it would work as he said guess what it works better! It is definitely worth the $50 he charges. I have one on a rifle charge bar and will get one for a pistol charge bar when it is time to load pistol. http://www.uniquetek.com/site/696296/product/T1231

  5. I was having problems with my new RF-100. WSPM primers would get stuck under the stabilizer plate in the last inch before dropping into the tube. It appeared that the anvils were sticking against the small bump on the bottom of the "A" stabilizer plate. I carefully removed that bump, but that only led to flipped primers (I'd get 2-3 upside-down per 100).

    I called Dillon and told them what happened. They sent me a new plate. I put it in and it did the same sticking thing. Knowing that not having the bump at all was causing flipped primers and having the bump was catching the primers, I decided to try a "mid-range fix".

    I took a target paster and stuck it to the bottom of the stabilizer plate, just enough to lift the plate approximately .010 inch. I cut out a hole in the paster for the screw, trimmed off the excess, and re-attached it. The thickness of the paster was enough to lift the stabilizer and allow the anvils to clear.

    The machine will now perfectly load a 100 primer tube in 35-40 seconds, consistently.

    I thought about switching to the "B" stabilizer. That may work, but what I made by grinding off the bump was essentially a "B" stabilizer, so I don't know if I would have still had the flipping problem.

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